diff options
author | Dom Cobley <popcornmix@gmail.com> | 2021-03-18 17:13:28 +0100 |
---|---|---|
committer | Maxime Ripard <maxime@cerno.tech> | 2021-04-08 14:55:02 +0200 |
commit | eb9dfdd1ed40357b99a4201c8534c58c562e48c9 (patch) | |
tree | c11703da04a123e5780ee43f42111d84cc26c540 /drivers/gpu/drm/vc4 | |
parent | 35d65ab3fdba1bdecde9ac3424d6d634ea038729 (diff) |
drm/vc4: crtc: Reduce PV fifo threshold on hvs4
Experimentally have found PV on hvs4 reports fifo full
error with expected settings and does not with one less
This appears as:
[drm:drm_atomic_helper_wait_for_flip_done] *ERROR* [CRTC:82:crtc-3] flip_done timed out
with bit 10 of PV_STAT set "HVS driving pixels when the PV FIFO is full"
Fixes: c8b75bca92cb ("drm/vc4: Add KMS support for Raspberry Pi.")
Signed-off-by: Dom Cobley <popcornmix@gmail.com>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Link: https://patchwork.freedesktop.org/patch/msgid/20210318161328.1471556-3-maxime@cerno.tech
Diffstat (limited to 'drivers/gpu/drm/vc4')
-rw-r--r-- | drivers/gpu/drm/vc4/vc4_crtc.c | 17 |
1 files changed, 17 insertions, 0 deletions
diff --git a/drivers/gpu/drm/vc4/vc4_crtc.c b/drivers/gpu/drm/vc4/vc4_crtc.c index 269390bc586e..76657dcdf9b0 100644 --- a/drivers/gpu/drm/vc4/vc4_crtc.c +++ b/drivers/gpu/drm/vc4/vc4_crtc.c @@ -210,6 +210,7 @@ static u32 vc4_get_fifo_full_level(struct vc4_crtc *vc4_crtc, u32 format) { const struct vc4_crtc_data *crtc_data = vc4_crtc_to_vc4_crtc_data(vc4_crtc); const struct vc4_pv_data *pv_data = vc4_crtc_to_vc4_pv_data(vc4_crtc); + struct vc4_dev *vc4 = to_vc4_dev(vc4_crtc->base.dev); u32 fifo_len_bytes = pv_data->fifo_depth; /* @@ -238,6 +239,22 @@ static u32 vc4_get_fifo_full_level(struct vc4_crtc *vc4_crtc, u32 format) if (crtc_data->hvs_output == 5) return 32; + /* + * It looks like in some situations, we will overflow + * the PixelValve FIFO (with the bit 10 of PV stat being + * set) and stall the HVS / PV, eventually resulting in + * a page flip timeout. + * + * Displaying the video overlay during a playback with + * Kodi on an RPi3 seems to be a great solution with a + * failure rate around 50%. + * + * Removing 1 from the FIFO full level however + * seems to completely remove that issue. + */ + if (!vc4->hvs->hvs5) + return fifo_len_bytes - 3 * HVS_FIFO_LATENCY_PIX - 1; + return fifo_len_bytes - 3 * HVS_FIFO_LATENCY_PIX; } } |